Commer News:
Had to have the cylinder head off. A slight misfire, which I originally thought was points, plugs etc, was diagnosed as a total lack off compression in cyl 4. Turned out to be a burnt out exhaust valve. I say burnt out, in reality about a third of it's diameter was missing! Not sure if this is anything to do with using unleaded fuel, but will be using Lead Additive from now on. However, compression and the condition on the valves on 1,2 and 3 are absolutely fine. A mystery really. Bores are in fantastic nick too. Put back together again, she fired up first time of asking and is now running like a train.
The absense of a properly functioning (spongy) brake pedal has not stopped Chris Zarse and his good lady from travelling up to Shropshire for a weeks' motor caravanning holiday in the splendid accommodation afforded by the Commer. They should be back on friday, allowing me the weekend to have a serious look at the brakes before the trip up to Donington and the LMS. So that'll be about 1000 miles this month, not bad for an old 'un.